Disassembled tensioners and noted differences. However crankshaft rear oil seal bolt gave way under torque of 12 lbs. Now all work stops to helicoli the two long bolts attached to oil pan.
Thursday, April 26, 2012
Timing Chain Tensioners
Disassembled tensioners and noted differences. However crankshaft rear oil seal bolt gave way under torque of 12 lbs. Now all work stops to helicoli the two long bolts attached to oil pan.
Wednesday, April 25, 2012
Rear Oil Seal
Rear oil seal installed,
UPDATE: These bolts screw into what appears to be helicoil. I tried to torque them to spec and they failed at 11 pounds. Everything is on hold.
Oil pickup and sump cover attached.
Preliminary check of flywheel runout shows less than .005 runout at 4 inches from center of flywheel.
Pictures of jack shaft housing taken no clear indication of failure of integral bearings. Very little movement up, down or side to side noted.
Thursday, April 12, 2012
Waterpump Done
Decided to rebuild rather than purchase a water pump. With the help of friends and a press we got it done.
Side by Side comparison of old and new parts |
Cast flashing on bottom of impeller and bearings pressed out of basket |
Cast flashing removed noticed a ridge defect hope the gasket holds |
After trying to press the bearing into the cage first we realized you press the bearing ont the shaft first. |
Finished Product |
Tuesday, April 10, 2012
April Update
Even Bank fully installed |
Odd Bank all but #1 installed |
Torqued rods to 45 pounds, used ARP assembly lube non seemed to over stretch. Measured height of piston at compression height. Highest piston is .080 inches high. Measured height of gasket which is also .080 inches high, we assume that the compressed height of the gasket will be .040 inches leaving .040 height between value and piston.
Best guess is that we will have enough space given that we are looking for 9:1 compression.
Thursday, April 5, 2012
Crankshaft Balanced and Piston Install Begins
Finally got the crankshaft sorted out. Having destroyed the first one "gaming" the Hines machine and discovering that there are no 60 over bearings for the replacement crankshaft I sourced a third crankshaft and immediately sent it out for professional balancing,
The balance included the disk cover as well. There was some residual wax and residual dust that had to be removed.
The crank has been laid and the rod clearances measured.
Ring gap was verified and documented.
Rings were installed, and pistons installed.
Care had to be taken with custom pistons manufactured to account for intake and exhaust value movement. The prior pistons were flat dished and it may be that orientation was not as important.
Now rod orientation and piston orientation to match intake and exhaust relief is critical.
The heads are being line honed.
The balance included the disk cover as well. There was some residual wax and residual dust that had to be removed.
The crank has been laid and the rod clearances measured.
Ring gap was verified and documented.
Rings were installed, and pistons installed.
Now rod orientation and piston orientation to match intake and exhaust relief is critical.
The heads are being line honed.
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